So, this happened.
Last monday was supposed to be a great day: We were finally going to bring our mustang up for examination before getting a title here in the Netherlands.
Let me clear up a few things first: I recently replaced the water temp. and fuel gauges because they were broken. Since I saw that they gave a reading which in my opinion looked OK given the current conditions I took it for granted that they were now working (Stupid me).
The examination centre was about 20 miles down south from where I live meaning that we had to go on the highway for the very first time. We decided to drive 50-60 mph without stressing the engine too hard. Halfway there we noticed that the temperature gauge gradually was increasing to hot. Once it reached hot we decided to stop, let it cool and check if anything was wrong. First thing I noticed was that our radiator was overflowing hot coolant through the radiator venting tube on the ground. Our fans (2x SPAL 13A, 1x SPAL 11A for tranny rad cooling) were spinning too. We did add extra coolant last saturday so I had a feeling it was related to that, hence we decided to continue driving.
About 5 miles further we had to take a turn and merge into another lane so we gave a little more gas and that's where everything went south. We heard a loud bang coming out of the exhaust followed by another bang which we have not yet determined. "Luckily" I made a video while it happened:
After this we were forced to pull over and check for any leakage or broken stuff (such as melted fuses), since we didn't find anything wrong we decided to crank it again but no luck. So we had to tow towards the examination centre, once we arrived we were not able to make it start again EVEN with a battery booster the starter was not able to make it run. As dissappointed as we are we had narrowed the issue down to not having a spark coming from the coil. We did notice some of the coolant sprayed over the engine block.
My theory while driving back (we got picked up) was that some of the coolant sprayed over the magnetic pickup connector causing a short in the distributor thus not triggering the electric ignition controller.
Once home I ripped out the electric ignition control and started debugging the issue with the troubleshooting guide made by MSD. I was able to generate a spark using a jumping wire:
Which leds me believe that something is up with the distributor itself. While doing some research I saw some horrific cases where the distributor gear on the cam was totally shredded. I certainly hope this is not the case for us. Next thing I will do is take off the distributor cap and maybe the distributor as a whole. Does anyone have some advice on what I should do? Is a whole engine teardown and rebuild required?
The setup we are running is as follows:
MSD 6AL-2 ignition control (MSD 6421 MSD 6AL-2 Ignition Control)
MSD 8478 Ford 351W Street Pro-Billet distributor (MSD 8478 Ford 351W Street Pro-Billet)
Holley 4781C 850CFM Double Pumper carb (Holley 0-4781C 850 CFM Double Pumper Carburetor)
351W block with Trickflow aluminium cyl. heads[/MEDIA]
Last monday was supposed to be a great day: We were finally going to bring our mustang up for examination before getting a title here in the Netherlands.
Let me clear up a few things first: I recently replaced the water temp. and fuel gauges because they were broken. Since I saw that they gave a reading which in my opinion looked OK given the current conditions I took it for granted that they were now working (Stupid me).
The examination centre was about 20 miles down south from where I live meaning that we had to go on the highway for the very first time. We decided to drive 50-60 mph without stressing the engine too hard. Halfway there we noticed that the temperature gauge gradually was increasing to hot. Once it reached hot we decided to stop, let it cool and check if anything was wrong. First thing I noticed was that our radiator was overflowing hot coolant through the radiator venting tube on the ground. Our fans (2x SPAL 13A, 1x SPAL 11A for tranny rad cooling) were spinning too. We did add extra coolant last saturday so I had a feeling it was related to that, hence we decided to continue driving.
About 5 miles further we had to take a turn and merge into another lane so we gave a little more gas and that's where everything went south. We heard a loud bang coming out of the exhaust followed by another bang which we have not yet determined. "Luckily" I made a video while it happened:
After this we were forced to pull over and check for any leakage or broken stuff (such as melted fuses), since we didn't find anything wrong we decided to crank it again but no luck. So we had to tow towards the examination centre, once we arrived we were not able to make it start again EVEN with a battery booster the starter was not able to make it run. As dissappointed as we are we had narrowed the issue down to not having a spark coming from the coil. We did notice some of the coolant sprayed over the engine block.
My theory while driving back (we got picked up) was that some of the coolant sprayed over the magnetic pickup connector causing a short in the distributor thus not triggering the electric ignition controller.
Once home I ripped out the electric ignition control and started debugging the issue with the troubleshooting guide made by MSD. I was able to generate a spark using a jumping wire:
The setup we are running is as follows:
MSD 6AL-2 ignition control (MSD 6421 MSD 6AL-2 Ignition Control)
MSD 8478 Ford 351W Street Pro-Billet distributor (MSD 8478 Ford 351W Street Pro-Billet)
Holley 4781C 850CFM Double Pumper carb (Holley 0-4781C 850 CFM Double Pumper Carburetor)
351W block with Trickflow aluminium cyl. heads[/MEDIA]